One of our club's MRC Tech II 2500s has "lost it's zero"...we cannot shut the power off to keep (most) engines from continuing to run. I see no external zero adjust...is there a way to open the pack (I know URL doesn't like that) and reset zero. Or do I just have to figure out a circuit to shunt some current?
Thanks for any help on this...
Your problem is different than this
http://cs.trains.com/mrr/f/744/p/274270/3126023.aspx#3126023
I don't think you are going to find anything adjustable inside.
The screws on my 2400 look like Torx. You would need something like this to open it up.
https://www.harborfreight.com/3-pc-saemetrictorx-folding-hex-key-set-61921.html
Henry
COB Potomac & Northern
Shenandoah Valley
Redvdub1 One of our club's MRC Tech II 2500s has "lost it's zero"...we cannot shut the power off to keep (most) engines from continuing to run. I see no external zero adjust...is there a way to open the pack (I know URL doesn't like that) and reset zero. Or do I just have to figure out a circuit to shunt some current? Thanks for any help on this...
I have the same issue- It had been in storage for a while. When I hooked it up it is still sending a little bit of current to tracks when it should be at 0. My first guess is that the rheostat has went bad. I suspect itis the rheostat and I would imagine that these are not going to be something we can find. With two people having the issue there must be others- wonder if anyone has been able to fix one? Jim
IF it's just the main potentiometer, you can buy one of the same value and possibly repair it. The biggest problem is there is no schematic available to help troubleshoot it. It could also be the main drive transistor gone leaky, or parts of the pulse system, not suppressing the pulse at 0 throttle.
--Randy
Modeling the Reading Railroad in the 1950's
Visit my web site at www.readingeastpenn.com for construction updates, DCC Info, and more.
drgwcs I have the same issue- It had been in storage for a while. When I hooked it up it is still sending a little bit of current to tracks when it should be at 0. My first guess is that the rheostat has went bad. I suspect itis the rheostat and I would imagine that these are not going to be something we can find. With two people having the issue there must be others- wonder if anyone has been able to fix one? Jim
I had this happen to one of my MRC Railpowers, between the two wiring guys in our club, they got it fixed. It is great to have experts like them. The actual part doesn't cost more than a couple of bucks though.
Harrison
Homeschooler living In upstate NY a.k.a Northern NY.
Modeling the D&H in 1978.
Route of the famous "Montreal Limited"
My YouTube
AttuvianWhere are you Mel?
If it has a potentiometer you might try cleaning it with an electronic parts cleaner. Make sure the cleaner is plastic safe. I have used CRC QD electronic cleaner.
This cleaner also works great on wheels and electrical pickups.
Bunch of parts off the board - there's another flying resistor on the direction switch, whatever that could be for. And another across 2 of the terminals of the momentum switch.
Hardest part about figuring it out would be getting a look at the other side of the board. Can;t just pull it out, with all those components soldered right between the board and a switch, and those switches aren't coming out, the plastic is melted in the mounting holes to secure them. I suspect it's a fairly simple momentum throttle circuit though, nothing super special (MRC's marketing nothwithstanding). Brake switch connects the momentum capacitor in the normal position, in brake it discharges the capacitor through that resistor. Color coding of the wiring, what color coding, it seems all over the place. Each of the pilot lights justs used the white wires the lights come with, you can see the two from the power light just parallel across the variable DC output, which are yellow and black wires. Another pair of white wires going to the momentum switch is the momentum indicator light. Be interesting to see what's going on witht he momentum circuit, as the left side terminals of that switch have the white wires for the indicator and also 2 yellow wires, one of which appears to go to one of the AC terminals ont he back, and the other to somewhere on the board. The other side has a green wire which goes under the board near the green component - probably the cap. And a black wire that is soldered to the board near the bottom center, next to the hole, and the large red wire coming from the transistor. Looking at the direction switch, it looks like the variable DC comes off the board in the upper left, the red and white wires.
It does look slightly familiar - I must have opened up my 1500 at some point.
This thread got split up so I will add to this thread segment my final findings.
Opening up the 2500 seemed to cure the "leakage" or "residual voltage" problem. I was able to reassemble the unit and it now works well..time will tell. I did findthe Darlington Tx literally submerged in heat sink grease and I cleaned it off and reapplied grease upon reassembly..but I hardly think sink grease could cause leakage across the TX leads. Upon reassembly (and after I ascertained the unit was working ok) I cleaned off the circuit board with isopropyl and a Q-Tip.
I believe the MRC Tech II 2500 utilizes a non center-tap Xformer, a 4 diode bridge rectifier, and a 2500-3000 ohm wire wound potentiometer (to feed the base of the Darlington Tx) as the essential "guts" of the power supply. There are two trim pots and two electrolytic capacitors to filter the rectified DC signal. The pulsing is (reportedly-not by my measurements) 60 Hz and as the throttle (aka potentiometer) is rotated from zero to full throttle the filtering is increased so as to remove all/most of the ripple.
My best guess as to the fault mechanism is that a leakage path developed across the Tx so that the potentiometer could not turn off the Tx completely. The most obvious causes would be either dendrite or whisker formation on the circuit board or the Tx leads. I feel a board defect is more likely.
Thanks for everyone's help and suggestions...much appreciated.
thanks for posting the diagram.
That along with the picture in the other thread may be enough to create a schematic
greg - Philadelphia & Reading / Reading
One final (perhaps) note on the 2500 problem. I think this supply is voltage regulated and those two trim pots are to adjust the output + and - voltages..
They weren't the problem..as you can see from the attached postings.
I just noticed I didn't follow up this posting. We solved our "leakage"problem by removing the circuit board and rinsing it off with isopropyl. It looked like there was quite a bit of residual flux between the solder pads and I suspect there was dendrite formation between the pads ...hence the leakage. Once removed I think we're good to go...
redvdub1
George T. Galyon
i thought dendrite formations occur within a battery. I don't understand why dendrites would form on a circuit board and would be washable with alchohol.
since the flux has been there since manufacture, does it attract the accumulation of dirty film that is conductive? will the problem re-occur over time? would the problem have occured if the flux were removed during manufacture?
it's interesting that simple cleaning fixed the problem (see overmod's comment regarding cleaning flux residual under thread on soldering)
Tin whiskers perhaps - but those things were made long before RoHS, so that solder should be leaded, the whole reason lead was added to tin solder was to prevent whiskers. But tin whiskers isn't just a new thing since the advent of lead-free solder.