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Any News from Cheyenne on the 4014 Big Boy?

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Posted by Anonymous on Tuesday, April 26, 2016 12:22 PM

Could we please stop the back-and-forth about what is happening?

This thread is about the Big Boy 4014, not the polictics of the UP steam program and what has happened in past years. If that is what you so desire to discuss, keep the mud-slinging in private message, or start a new thread.

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Posted by stdgauge on Tuesday, April 26, 2016 11:11 AM

Shadow the Cats owner
I have gone back thru and watched the updates they have posted on youtube. In them they described how the Separator had quit working allowing scale and sludge buildup and that 3 different drainage tubes that were supposed to end up under the firebox instead had been routed into the firebox and various lines that should have been steel tubes had been replaced by rubber hoses by the last crew to run her. Sorry if your running a locomotive that has never been retired at all by your employer you do not jury rig repairs. I looked at my husbands old issues of Trains magazine when 844 was put back into service after her overhaul in the 90's by Steve Lee. Even on her Break-in run things did not sound right to me back then looking back. He was like she has a pair of Air Compressors she can run with one of them out of service or the Diesel helper can provide the air needed for the train. HELLO that is not how you run a railroad steam program.
 

 
Nope.  Sludge build-up was the result of current management changing water treatment and changing blow down equipment and frequency.  Don't believe some of the lies coming out of Cheyenne. 
 
Tender of 844 was severly damaged by the improper chemicals used by current manager also.  If you want proof, look at 3985's tender and boiler - no sludge, because current manager has not touched it.
 
Current manager HATES Steve because he was demoted by him and has been trying to blame EVERYTHING that has gone wrong on him or someone else.  It is THAT kind of garbage that I really hate. 
 
Then, there are the lawsuits.  Maybe after those are over in the fall, the hammer will come down on current manager!
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Posted by Shadow the Cats owner on Monday, April 25, 2016 3:44 PM
I have gone back thru and watched the updates they have posted on youtube. In them they described how the Separator had quit working allowing scale and sludge buildup and that 3 different drainage tubes that were supposed to end up under the firebox instead had been routed into the firebox and various lines that should have been steel tubes had been replaced by rubber hoses by the last crew to run her. Sorry if your running a locomotive that has never been retired at all by your employer you do not jury rig repairs. I looked at my husbands old issues of Trains magazine when 844 was put back into service after her overhaul in the 90's by Steve Lee. Even on her Break-in run things did not sound right to me back then looking back. He was like she has a pair of Air Compressors she can run with one of them out of service or the Diesel helper can provide the air needed for the train. HELLO that is not how you run a railroad steam program.
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Posted by Dr D on Sunday, April 24, 2016 10:37 PM

stdgauge,

Missing Fantrips!  Yes, I will grant you that there is more going on today about meticulious restoration of UP 844 into "museum piece" condition than gett'n her down the road on another excursion!  Possibly this restoration effort will become the ground work for real workable steam program in the future.  Imagine an engine of this restoration quality actually running though!

Whatever the case, you are not going to change Union Pacific's plans about having Ed Dickens in charge of whatever game they are up to by whining about it.  Clarity of vision is needed here.

Water Treatment and Boiler Blow Down Procedures or lack thereof also seem to be one of the main concerns about the damage to the FEF - as they are on all steam locomotives.  Just why this procedure was altered on UP 844 is unclear.

I believe the boiler blow down procedures may be changing as part of an Enviornmental Protection Agency concern for random toxic ground pollution covered under new guidelines limiting the locations and manor in which this can be performed. 

Similar enviornmental concerns govern the dumping of firebox waste ash and other combustion products onto the ground to say nothing of the oil and exhaust smoke pollution issues.  Hasn't California prohibited railroad steam locomotive exhaust?  Seems that many things we once took for granted like passenger car waste may now become some kind of future haz-mat issues.  The days of smoking it up for a fan trip run by surely must be over!  Possibly UP may have concerns over other looming politically correct issues.

-------------------------

I know Ross Rowland and have ridden in the cab of C&O 614 with him.  Rowland and McCormack, however knowledgable do not constitute the responsibile, opinions and decisions of a Class 1 railroad like Union Pacific.

------------

Yah, I heard the part where Ed Dickens talks about being a M60 machine gunner in the Army.  I would think they would have chosen a former Army officer for leadership in a managment position such as the UP steam shop.  A US Army sergeant might make a better foreman than a steam program director.

-------------------

It is what it is!

Doc

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Posted by stdgauge on Sunday, April 24, 2016 8:58 PM

Dr D

stdgauge,

I have done most of the steam mechanical activities that Ed Dickens and crew are doing on UP 844 only I worked on PM 1225. 

Replacing and installing the large studs into the boiler plate for accessory mounting, working on the boiler feed ball check valves and piping.  Reaming out the multiple throttle assembly, hanging the entire locomotive throttle from quadrant to valve head.  Removing the side rods and valve gear, working on the brake rigging.

I guess I never did large scale "hot riveting" like they are doing to the firebox interior. 

I have even turned the large brass main rod bushings on the huge shop lathe and done it to blueprint spec. 

I find little or nothing to complain about Ed Dickens and his work crew - in fact they have very high standards of work.

I feel bad that Union Pacific moved out your friends and "the former steam crew" but that's the company politics of getting fired. 

So do us all a favor and quit complaining about the "true steam crew," we are all stuck with the Ed Dickens administration and would like to enjoy this one spectacular steam restoration event in peace. 

As with any crew, all are different with different focus, different strengths and abilities - and the new Ed Dickens bunch is here even if they are more like museum conservators and curators.

I am just real dam glad that someone is rebuilding the 4-8-4 - any 4-8-4 to that degree of quality.  And they also have the entire class 1 Union Pacific railroad to run the locomotive on!  Try to find that anywhere else in the USA besides Cumbries & Toltec Senic RR or Durango Silverton RR.

Likely UP 844 will run the remainder of your and my lifetime!  I'm glad, arn't you?

--------------------

Doc

 

 
Umm, please read my comments again. 
 
1.  Where did I say they were "my friends?"  That's right, I did NOT. 
2.  I said that former UP employees (retired), AND SCORES of TRUE steam experts, with PROVEN track records have stated their concerns.  Most of these people have NOT worked for UP.  For example, one is at the head of the FWRHS, another at the head of Ross Rowland's team, another with Doyle McCormack's team, another with WRRC, etc. etc. 
 
3.  Quoting a true steam expert (Wes Camp) about the disaster of changing the blow down system that worked perfectly for DECADES: 
 
"Which alludes to another management principle:  
The definition of Stupidity:  Doing the same thing over and over, and expecting a different result"....... 

If the 844's water blow-down system is not made fully operational, as designed & intended,---- then continuing the failed water management scheme will fall into the trap of: " ...expecting a different result...."

We may get to see a real-life example of Stupidity, defined..... "  AND Wes Camp  did NOT work for the UP.
 
4.  You can ignore and deny the facts all you want, but I won't.  I am VERY concerned, and I want nothing more than to see UP steam succeed.  If you want a quality rebuild, you do it right, like FWRHS, Friends of 4449, etc. Funny how these volunteer groups, without having the financial resourses of a class 1 railroad, can accomplish all that they do because they have the RIGHT people in place.  Hint, hint!
 
As for your tone and comments I say "There are none so blind as those who will not see." 

 

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Posted by ROBERT WILLISON on Sunday, April 24, 2016 10:33 AM

Doc, we don't always agree, but this time you nailed it. Company culture  is company culture. Its time to stop listening to rumors and let the up get on with it.

I don't know if everyone one  saw up latest financial results. But they took a big hit, we are lucky they haven't scaled back their steam program like ns has.

So less complaining and  bit more support. Their are far worse possible out comes out their.

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Posted by Dr D on Sunday, April 24, 2016 1:03 AM

stdgauge,

I have done most of the steam mechanical activities that Ed Dickens and crew are doing on UP 844 only I worked on PM 1225. 

Replacing and installing the large studs into the boiler plate for accessory mounting, working on the boiler feed ball check valves and piping.  Reaming out the multiple throttle assembly, hanging the entire locomotive throttle from quadrant to valve head.  Removing the side rods and valve gear, working on the brake rigging.

I guess I never did large scale "hot riveting" like they are doing to the firebox interior. 

I have even turned the large brass main rod bushings on the huge shop lathe and done it to blueprint spec. 

I find little or nothing to complain about Ed Dickens and his work crew - in fact they have very high standards of work.

I feel bad that Union Pacific moved out your friends and "the former steam crew" but that's the company politics of getting fired. 

So do us all a favor and quit complaining about the "true steam crew," we are all stuck with the Ed Dickens administration and would like to enjoy this one spectacular steam restoration event in peace. 

As with any crew, all are different with different focus, different strengths and abilities - and the new Ed Dickens bunch is here even if they are more like museum conservators and curators.

I am just real dam glad that someone is rebuilding the 4-8-4 - any 4-8-4 to that degree of quality.  And they also have the entire class 1 Union Pacific railroad to run the locomotive on!  Try to find that anywhere else in the USA besides Cumbries & Toltec Senic RR or Durango Silverton RR.

Likely UP 844 will run the remainder of your and my lifetime!  I'm glad, arn't you?

--------------------

Doc

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Posted by Shadow the Cats owner on Saturday, April 23, 2016 7:37 AM

I fired off a question on the amount of asbestos found on the 844 and 4014 via the Facebook group and wheter they knew about the asbestos on 4014 when they took it from CA.  The answer I got back was they where fully aware of all the Asbestos on the 4014 and where going to remidiate during its overhaul as scheduled.  They found close to 60 Lbs of asbestos total on 844 and they had paperwork signed off by Steve Lee himself stating that all asbestos had been removed in the 70's by certified personal.  

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Posted by stdgauge on Friday, April 22, 2016 11:57 AM

Shadow the Cats owner
I went over all the reports I found in the Facebook 844 group. They did find asbestos on the 844 in the air brake stand. It had never been apart in the last 60 years. Some of the packing in it was asbestos according to both a video and other people. 60 years without tearing apart the brake stand. As for your turnover question why has it been higher easy the new guy has instituted Quality control on the work plus is demanding someone be held accountable for their work for the first time in years. I guess no one ever had to be held responsible if it broke down on the road. He wants a reliable engine on the road away from Cheyenne. The sludge in the boiler they found so much other stuff wrong with the boiler that the sludge was the least of their concerns. Stuff like Busted Stay bolts improper mounted stays also 2 of the 4 washout plugs had not been removed for 30+ years how do they know that from the amount of Rust on them. They literally had to cut them out of the boiler. The Stays that where broken not one had the weep hole in them so they only found them broken when they tore down the boiler. The tool car getting damaged was an accident.
 

1.  Tool car - an accident that was HIS responsibilty. 
2.  Improper mounted stays - discussed at lenght elsewhere and was determined by the TRUE steam experts to be fine.
3.  Asbestos in the brake stand of 844 - IF true, a very small amount compared to the large amount on 4014 that was MISSED by you know who.
4.  "Sludge the least of their concerns"  Did you really say that?  Wow.  That was/is a HUGE problem, and a potential Gettysburg in the making.  There is NO reason that should have happened.  He changed the chemicals and the blow down procedures and equipment, and they caused this problem.  WRONG thing to do.
5.  "He wants a reliable engine on the road away from Cheyenne."  His track record of flat-spotting the wheels and changing the story multiple times as to how it happened?  Guess what REALLY happened?  The nut on the seat box forgot the MU box was set to Run 6. 
6.  #2 Diesel was used by the current management as the fuel source, against the recommendation of all the experts.  Guess what?  THAT is what screwed up the firebox, because it heats VERY unevenly.
7.  Rod bearings were replaced by current management, but were spec'd at 1/2 the tolerances specified on the UP Mechanical Department drawings.  Guess what?  The rod bearings ran hot, but he blamed it on the pin grease.  NO.  Why would anyone change what was spec'd on the drawings!?!?  Not smart. 
 
Sorry, I really want UP steam to succeed, but I am VERY concerned.  I base my concern on the concerns of MANY, MANY knowledgeable steam experts that have DECADES of experience with proven track records.  All these people are concerned, so I am too.  Who would you trust?  One person, or scores of people that have decades of proven track records? 
 
I hate to say, but something is VERY wrong in Cheyenne.  Open your eyes and mind, and you'll see.
 
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Posted by Shadow the Cats owner on Friday, April 22, 2016 11:39 AM
4014 right now is still in one piece for the most part from what I can gather. UP is not doing anything on her until 844 is back up and running. The order of repairs is 844 4014 then 3985.
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Posted by stdgauge on Friday, April 22, 2016 11:27 AM

What about all of it that he missed on 4014???

Sorry, too many stories coming out of Cheyenne.  I trust the true, proven experts.

 

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Posted by Anonymous on Friday, April 22, 2016 9:27 AM

stdgauge

 

 
S. Connor

Don't forget the asbestos they found on 844 too...

 
WRONG.  It was found on 4014 AFTER it was moved back to Wyoming.  Yet another error....

Tell that to Mr. Dickens. From the man himself, they found asbestos on 844: https://youtu.be/YsPl73r6i18?t=11m37s

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Posted by Shadow the Cats owner on Friday, April 22, 2016 7:52 AM
I went over all the reports I found in the Facebook 844 group. They did find asbestos on the 844 in the air brake stand. It had never been apart in the last 60 years. Some of the packing in it was asbestos according to both a video and other people. 60 years without tearing apart the brake stand. As for your turnover question why has it been higher easy the new guy has instituted Quality control on the work plus is demanding someone be held accountable for their work for the first time in years. I guess no one ever had to be held responsible if it broke down on the road. He wants a reliable engine on the road away from Cheyenne. The sludge in the boiler they found so much other stuff wrong with the boiler that the sludge was the least of their concerns. Stuff like Busted Stay bolts improper mounted stays also 2 of the 4 washout plugs had not been removed for 30+ years how do they know that from the amount of Rust on them. They literally had to cut them out of the boiler. The Stays that where broken not one had the weep hole in them so they only found them broken when they tore down the boiler. The tool car getting damaged was an accident.
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Posted by stdgauge on Thursday, April 21, 2016 8:32 PM

S. Connor

Don't forget the asbestos they found on 844 too...

 

WRONG.  It was found on 4014 AFTER it was moved back to Wyoming.  Yet another error....
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Posted by stdgauge on Thursday, April 21, 2016 8:31 PM

Sorry, I hear a lot of "stuff" coming from Cheyenne, and it is not adding up.  I trust people like Wes Camp, Steve Lee, Bob Krieger, Jack Wheelihan, the whole WRRC group, etc.

They've been working on and with steam locomotives for decades, and have a great track record.  They've also proven MANY things that have been said from the current group wrong.  And there are other sucessful steam operators who say the same thing - the current UP Steam shop is not good!

Let's look at just a few examples recently:

1.  Turnover at the UP Steam shop has been 200% in recent years

2.  The fact that the boiler of 844 is full of sludge is due to changing long-successful water treatment programs and not doing proper blow-downs.

3.  Flat-spotting the drivers

4.  Wrecking the tool car

5.  Others, which i won't go into here

I am hoping for the best, but I fear the worst until some things (people!) change in Cheyenne.

 

 

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Posted by Anonymous on Thursday, April 21, 2016 10:45 AM

Don't forget the asbestos they said they found on 844 too...

 

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Posted by Shadow the Cats owner on Wednesday, April 20, 2016 4:15 PM

I joined the 844 community on Facebook they are got all 58 tubes reinstalled in her plus started on all the Superheaters they said.  From what was being said in previous updates of what they found in teardown that problems were being hidden.  The airbrake stand had not been rebuilt for 60 years some of the piping under the cab was original according to some with inside knowledge.  The kicker was what they found with some of the parts that Steve Lee supposedly rebuilt in 1994.  They had just been repainted not stripped and gone thru.  They found studs corroded off and other issues that were older than the last Overhaul.  In one video the new guy claims that part of the reversor what ever that is had so much wear in it they were amazed that it even worked.  

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Posted by csx6000 on Friday, March 4, 2016 7:40 AM

that is what I head too, but I would have liked to see the locomotive operate with caol first

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Posted by Wizlish on Monday, February 29, 2016 7:16 PM

blue streak 1
Here is a minor update on both 844 & 4014. Rebuilt brake control & stand. Any one know what the brake type is ( such as 26L ) ?

Clearly labeled in the video as an 8ET.  His choice of words explaining what the automatic brake system does is a bit strange, as if it were unfamiliar.

 

I hope everyone noted the last few sentences about how they have all the 'subassemblies' done and are going to start bolting the locomotive back together ... that shuld not really take them all that long, if all the 'quality assurance' stuff has been done.

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Posted by BaltACD on Sunday, February 28, 2016 7:18 PM

844

Never too old to have a happy childhood!

              

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Posted by SD70M-2Dude on Sunday, February 28, 2016 12:22 PM

Holy crap they really are going authentic, I would have thought for sure they would convert to a 26L for commonality with the rest of their diesel fleet. 

Greetings from Alberta

-an Articulate Malcontent

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Posted by stdgauge on Saturday, February 27, 2016 1:02 PM
I read elsewhere that It is an 8ET.
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Posted by blue streak 1 on Saturday, February 27, 2016 4:08 AM

Here is a minor update on both 844 & 4014.  Rebuilt brake control & stand. Any one know what the brake type is  ( such as 26L ) ? 

http://www.up.com/aboutup/community/community_ties/steam-update-2-26.htm

 

 

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Posted by BENJAMIN DEUTSCHMAN on Saturday, December 12, 2015 11:48 AM

I'd love to see even minor updates, anything.

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Posted by BaltACD on Monday, November 23, 2015 12:55 PM

Dr D

Yes, I forsee a time when UP steam excursions will not be pulled by sleek passenger engines with all air conditioned coaches - Yes, I forsee a time when a "new age" steam excursion will have paying passengers to just ride in the boxcars and the open gondolas pulled at 20 to 40 mph by UP 5511 or UP 9000 with a hot coffee pot in the Union Pacific wooden caboose - with a hobo guitar player struming "This is Your Land This is my Land!"

UP 4023 vs. UP 5511 - as fates would have it!  Victory not always to fastest, the biggest or the most deserving - that's IRONY my friend!  It's the experience of the human heart where nothing really makes sense but just being a falliable human is the only thing that makes sense!

Doc

Good luck in finding Depression Era freight cars for your steam powered drag freight to haul.

Never too old to have a happy childhood!

              

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Posted by daveklepper on Monday, November 23, 2015 3:10 AM

I applaud both the NS and UP programs and applaud BNSF's allowing others to steam on their lines.  I hope all this continues, and generates far more applause than criticism.

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Posted by Dr D on Monday, November 23, 2015 1:28 AM

I hear you Leo!  

And do you want to know the greatest IRONY of them all!  UP 4023 BIG BOY had the lowest mileage of any of the 4-8-8-4 locomotives. The railroad wanted to save one for possible operation so they chose UP 4023 and overhauled her to good condition - then stored her inside the Cheyenne backshop to await future events to unfold.

UP 5011 2-10-2 starred in the company movie "Last of the Giants" then was ordered scrapped - they cut her piston rods with the oxy-acetylene torch!  Some junior executive, shop forman, somebody just never filled out her paperwork and sent her to scrap!  So UP 5511 just sits there today in the backshop with no record of her existance on paper - at least there wasn't for years - waiting for the future and untold events.

So which engine makes it into possible operating condition today?  The giant Big Boy UP 4023 groomed for destiny?  The lowly freight drag hog UP 5511 Texas type with one foot in the melting furnace?  Shades of the race horse "Seabiscuit!"

As fates would have it - misguided managment puts UP 4023 outside to waste in the rain and weather and UP 5511 hiding in ignominity in the backshop corner comes through to be a real candidate for future restoration!

Whenever I think about this, I also think I'll turn up a few Woodie Guthrie ballads - in honor of UP 5511 - songs like 

"This Land Is Your Land" - "Hobo Lullaby" - "Worried Man Blues" - "Goin Down The Road Feeling Bad" - "Hard Travelin" - and "Pastures of Plenty!" 

 - and dream of the day I will see UP 5511 on a drag freight with a few hobos - myself included - riding the boxcars - surely UP 5511 would accomplish something here that the mighty UP 844 would not - to be a lowly drag freight engine of the Great Depression era!

Yes, I forsee a time when UP steam excursions will not be pulled by sleek passenger engines with all air conditioned coaches - Yes, I forsee a time when a "new age" steam excursion will have paying passengers to just ride in the boxcars and the open gondolas pulled at 20 to 40 mph by UP 5511 or UP 9000 with a hot coffee pot in the Union Pacific wooden caboose - with a hobo guitar player struming "This is Your Land This is my Land!"

UP 4023 vs. UP 5511 - as fates would have it!  Victory not always to fastest, the biggest or the most deserving - that's IRONY my friend!  It's the experience of the human heart where nothing really makes sense but just being a falliable human is the only thing that makes sense!

Doc

 

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Posted by Leo_Ames on Sunday, November 22, 2015 11:14 PM

Dr D
They put 4023 outside to be destroyed by the elements and they began operating in a very small space with very little equipment.  

Frusturating to think about, since 30 years ago or so, she'd of been in the best shape of the bunch. Now, she rivals the example at Steamtown for being in the worst shape and was at the bottom of the list when Union Pacific initiated this project.

I'm glad the 3985 escaped after a few years of outside display in Cheyenne. I think she only was static after being kicked out of the roundhouse for 4 years before work started on resurrecting her.

Otherwise, she'd be in the same shape today. 

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Posted by Dr D on Sunday, November 22, 2015 10:50 PM

I can remember visiting the UP steam shop in 1968 just 4 years after the last of the steam era.  In 1968 it was a marginal operation!  Yes they had UP 8444 running as a public relations locomotive - but it was amazing they were able to keep it going.  

The roundhouse was in-tact and so was the huge locomotive backshop which housed 3895 Challenger and 4023 Big Boy and the lost 2-10-2 Texas type UP 5511.  But the gigantic overhead crane was the ONLY THING that remained in that entire Cheyenne steam backshop built to overhaul at least 40 locomotives - it was entirely and completely empty!  

I can remember thinking at the time - "Why wouldn't they have saved at least a rudementary of tools - yes, UP 8444 was living on a corporate good wish and a prayer.  

Since that time during the so called "UP great steam train era" they tore down half the backshop and roundhouse.  They put 4023 outside to be destroyed by the elements and they began operating in a very small space with very little equipment.  

For crying out loud they couldn't even turn locomotive drive wheels and had to take UP 844's flat drivers put them in a gondola and send the to the Strassburg RR in Pennsylvania!

Ed Dickens may be the target of much fan abuse but at least he is presiding over a complete backshop rebuild including massive tooling including the overhead crane and the planned operation of at least three steam railroad giants on an continuing basis.

I foresee the day when UP could contract out the restoration of any steam locomotive in America if they wanted!  With newly acquired knowledge and expertise!

I think we need to give Union Pacific the benefit of the doubt here.  I realize when Ed Dickens does his videos, it's kinda for the "new age generation," that never saw steam operate in the historic period - and he kinda makes steam loccomotive overhaul look like he's running NASA instead of "beatin your life out with a hammer pounding on drive rods!"  

For crying out loud Union Pacific just double tracked half the American continent - how much does this truly modern railroad need to bleed to convince doubters?  

Furthermore take a lesson about life - the "romanticism about steam" - the romanticism about anything - is really all about the big expectations we have anyway - because nothing ever lives up to what our dreams would be like.

Doc 

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Posted by kgbw49 on Saturday, November 21, 2015 10:57 AM

Well stated. We already have four of the big seven railroads that for the most part want nothing to do with steam. If NS falls to CP it will be five. Meanwhile, one railroad is still willing to own, maintain and operate three 70+-year-old steam locomotives. And not just popguns, but each the equivalent of a 16 inch 50 caliber battleship gun for their category, all being both mountain climbers and fast runners to boot. As for me, I will wait patiently, purchase occasionally off their Web site to support the program, and then be thankful and applaud heartily when they next roll out of the roundhouse, because no matter when those days come, they will be good days indeed.

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