Copied from the Tranist Forum, Three Modern Streetcar thread:
Out of date
So what? How many experiences of riding Ed Ellis's service have been posted? Very few. I found it interesting and thus shared it. You don't have to read what does not interest you.
I would have posted it earlier if received earlier.
And you did not pay anything for it.
I merely stated a fact. You needn't get nasty. Be glad at least someone noticed your post. It should have stated when he rode these trains.
Then my apologies to you. I thought you were registering a complaint. But nearly all readers know Ed Ellis's experiment ended, and the posting does say so; and in fact, Jack's analysis is more recent. The trips took place on 28 and 29 September 2016.
I feel glad that I got to experience what Ed Ellis did with the Hoosier. I took it to Indy to participate in a Cincinnati RR Club's tour of Amtrak's Beech Grove Shops and the Indiana Transportation Museum (RIP). Unlike Jack, I elected to return to Chicago on the dog. It was faster even though it got off the Interstate to go into downtown Lafayette and Gary plus went to the 95th St CTA station enroute to Chigago. Bus had a governor that gave it a top speed of 67 mph on highway. Train speed was max of 60 mph with some stretches of 40 and 20 coming out of Chicago. Food was good, crew excellent. Four employees from Iowa Pacific (Chef, Server, and two coach attendents) and three from Amtrak. Amtrak normally would have just had an Engineer and conductor but this trip had an assistant conductor.
Thanks for your report. But how were timekeeping and general cleanliness?
daveklepper Thanks for your report. But how were timekeeping and general cleanliness?
OK Dave.
The Hoosier State left CUS on time and ran at speeds up to 40 mph on the UP (former C&EI} to Dolton, at which point it slowed to 20 mph. Passing UP's Yard Center it stopped at CP 1020, Then crawled through Thornton Jct onto the CN (former GTW) where we got up to 79 for the short run to the connection to CSX (former Monon) at Maynard. On CSX we did speeds up to but never exceeding 60 mph. Arrived all stops ahead of time and waited for the schedule departure time. Arrived IUS about twenty five minutes before the advertised. Had the line to ourselves (no meets) that night. Noted that the switch at Crawfordsville did not require us to stop and throw it as happened on a precvious trip on the Cardinal. Train was clean, coaches (3) were former long haul (I think SF) and were clean. Load leaving Chicago was about 75-100 coach and about 30 first class. Most of the coach load was LaFayette as I walked the train before Crawfordsville and found two coaches empty and the third had about 25 passengers.
Food was freshly cooked to order and tasty. My memory fails me as to what it was.
Thanks. Good report. A model.
Nice job Dave and charlie. The train might not have been successful from a financial point of view, it was an interesting experiment all the same.
For many of us, it reminded us of how passenger trains were ran pre amtrak by the private railroads. The good old days of Budd cars, diners and domes.
Always a good discussion.
There are rumors, the only reason the experiment failed, was IP missed a detail or two in the payments section of the contract when figuring costs. In other words they thought they were making money until it was pointed out.
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